Archive for the ‘Engine’ Category

Bolting stuff to the engine

Sunday, February 17th, 2008

This is the Precision Airmotive RSA-5 fuel injection servo. I need to get this guy bolted onto the airplane, but it didn't come with any instructions – so I don't know, for example, if I need a gasket between the servo and the oil sump, or what. I sent an email to Mattituck.

Van's makes a pretty well-done little kit that contains a bellcrank for connecting the mixture cable to the fuel servo, and a series of little brackets for anchoring the control cables to the engine. I removed two of the case bolts and attached the bellcrank bracket to the oil sump, like so:

The mixture cable bracket attaches via another pair of case studs, underneath the #4 cylinder. These nuts all have lockwashers under them.

The throttle cable bracket bolts to a threaded boss on the bottom of the oil sump. I safety-wired the bolt heads:

Those coarse-thread bolts didn't come drilled, so I had to use my handy bolt-head-drilling jig to do it myself:

Here we go, two drilled-head, coarse-thread bolts:

I attached the engine-driven fuel pump's inlet fitting:

…and the outlet fitting, with restrictor fitting to feed the fuel pressure transducer:


Hung the engine

Sunday, February 10th, 2008

With the engine suspended from the hoist, we unbolted and removed the pallet, leaving the engine swinging:

Matthew Brandes and his foreign-exchange student Nat came up to help put the engine on. Matthew has already been through this exercise on his RV-9A, so he is an old hand. We maneuvered the engine into place and managed to get the first three bolts in without much trouble, but the last one was kind of a goat-rope.

Chad was there to help too. Maybe he'll get started on his own RV soon…?

Finally, all four bolts went in. We unhooked the hoist and lowered the tail down before final-tightening the nuts.

I was able to get all four cotter pins put in, and considering that there's almost no access to install them, I'm happy with how they turned out.

The fuselage is on the wheels with the engine installed. Awesome.

The prop governor oil line comes pretty close to the engine mount. I'll have to keep an eye on this.

The oil filter looks like it's trapped forever, but there's just enough room to remove and reinstall it.

It took about an hour and a half for us to get the engine bolted to the mount, and another hour or so for me to get the bolts tightened, install the cotter pins, and clean up. All in all, much less work than I thought it would be. Thanks to Matthew, Nat, and Chad for the help.

Preparing to attach engine

Saturday, February 9th, 2008

Per the plans, I'm using Permatex #2 sealant on all threaded plumbing that attaches to the engine:

I had to remove the oil filter to install the fitting for the oil cooler return line:

With the filter back on, there appears to be plenty of clearance to get a hose onto this fitting without hitting the filter or magneto. The plans say to use a straight fitting here, but a 45-degree fitting is really necessary if you have an angled oil filter adapter like I do.

A crow's foot wrench came in handy for tightening the fitting for the other oil cooler line. A 45-degree fitting is necessary here too, as others have discovered.

Looking from the left side of the engine, you can see how the hose will go between the prop governor bracket and the engine-driven fuel pump. I may also have to use a hose with a 45-degree fitting on the end – we'll see.

Looking into the business end of a VA-128 restrictor fitting. The end is plugged with a brass (?) insert that has a small passage drilled through it. Using these for the oil and fuel pressure pickups is a smart idea, so that a broken transducer hose won't dump all your oil overboard or pump fuel onto the hot exhaust pipes.

The oil pressure fitting has to be clocked at a 45-degree angle to vertical, so the hose goes the right way and doesn't hit the engine mount. Notice I had to remove one of the clips that attaches the right magneto drive pad cover plate, in order to get a wrench on the fitting.

I propped up the tail with a sawhorse padded with foam rubber. The tailwheel spring is secured to the sawhorse with a bungee cord so it doesn't accidentally get knocked off.

Now the fuselage is roughly level, which will make hanging the engine easier.

I manhandled the engine pallet up onto dollies, and rolled it over towards the front of the fuselage:

Then I levered the whole works up onto the feet of the engine hoist. I'll unbolt and discard the pallet once my helper arrives tomorrow.

Heavy red thing is ready to attach to white thing.


Installed prop governor

Wednesday, February 6th, 2008

Here's the propeller governor, a PCU500X. This guy is basically an speed-controlled oil pump, which controls the pressure of the oil being pumped through the hollow crankshaft, and thus sets the pitch of the propeller blades to hold the desired RPM. I started to explain this to Mary but she was too distracted to endure another of my lectures about aviation theory, so I just told her "it costs a thousand dollars and makes the airplane go like hell."

I had to cut off the safety wire, loosen the screws, and rotate the shaft to the correct angle to fit Van's cable bracket. Here it is after I redid the safety wire:

I used my cool new Milbar reversible safety wire pliers to twist the new lockwire, and I must say the improvement in my safety wire workmanship is noticeable compared to when I was using the old, cheap pliers. I guess once again I learn that quality tools make a difference.

I wiped down the surface of the governor drive pad, and removed the caps covering the drive gear and the oil ports:

Likewise, I cleaned the mating surface on the governor and removed the plastic plugs from it too. I made sure to take these photos so I don't have to wonder, "did I really remember to remove those plugs before I bolted on the governor?"

The instruction sheet that comes with the governor says to coat both sides of the included gasket with "a suitable release agent". I dithered on this for a while before finding an old RV-List posting mentioning that Van's preferred substance is plain old fuel lube. I guess the idea here is to make it possible to remove the old gasket if you have to remove the governor, and not to put something on there to enhance the quality of the seal (e.g. Permatex).

Then I bolted the governor and cable bracket to the engine, using star washers under the nuts. Due to the clearances involved I had to use a crow's foot on my torque wrench when tightening the nuts, but that was no big deal.

Here's the model info and serial number, in case I ever need it: